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BuiltWithNOF
Headstock

The headstock is very simple but I was never very impressed with the 3 step cone pulley. From the minute I set eyes on it - it looked wonky and unfortunately the lathe did vibrate annoyingly when running.

The original headstock

I managed to remove the chuck and backplate quite easily but the spindle wouldn’t push through from the front. It was clear I had to remove the back nut and the brass spacing ring between the nut and the rear bearing.

Nut on the end of the spindle

Not being able to get the nut to unscrew I resorted to clamping both the end nut and the spacing ring with an adjustable spanners/wrenches and hacksawing the spindle through with an HSS blade.

Removing the brass ring from around the steel shaft

With the nut and the spacer ring removed the spindle was easily knocked out with a mallet.

Knocking out the spindle

I happened to have a couple of nice aluminium single pulleys with a central hole very close in size (about .5mm) to the original pulley. Fortunately the original pulley didn’t fit tightly but instead relied on a sleeve insert which I reused.

I also had to cut down an M5 machine screw to turn into a set screw for the new pulley.

New pulley on left and old on right

After a little adjustment of the set screw and the addition of a hose clip or two the new pulley worked fairly well. Its a bit limited with only 1 speed so I’ll probably build a counter shaft at some point although for the moment 1 speed in the 500-1000 RPM range will probably do.

The new pulley however did show up just how much of the vibration problem was down the the V belt and I will replace this belt as a matter of urgency. I may try the original pulley again sometime - although I have figured out a sensible countershaft arrangement to work with this single pulley.

New pulley fitted


Final job is to make a new  end nut (5/8” BSW). In the end I used a piece of plastic (nylon). Once the lathe is sorted out - I’d like to redo this with a nice bit of brass.

Boring out new end cap


Initially I used my
Wizard lathe to bore it out so I could tap it 5/8” BSW. However I didn’t get the thread straight enough - so I rebored it further to a clearance fit.

The front was turned down to match an aluminium ring that was already just about the right size and the back turned down and slit to take a hose clip.

The finished plastic part


In the picture below I’m turning down the rim of the aluminium ring so only the central part makes contact with the back of the bearing.

Turning down the aluminium ring


A little superglue holds the ring and plastic together

The aluminium ring - mounted

The final result. A quick test shows the whole assembly hangs together fine.

The whoel assembly fitted to the lathe

This should have been the end of this page - but careful checking shows the front of the spindle catches very slightly on the split bearing. This will definitely cause vibration - so I’m going to insert a precise brass ring between the two which hopefully will make it run just that little bit smoother.

 

All text and images Copyright © 2000-2010 Roland Givan, unless otherwise stated. All Rights Reserved. Game artwork copyright their respective publishers.

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